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Old 15-10-2017, 09:20 PM
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dazdavies dazdavies is offline
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Good job I was planning that winter refresh on the engine. Pity the dropped valve beat me to it.

I've stripped the block down this morning. Bearings were on their way out. Rear thrust bearing, both halves were cracked!!

I've had zero mechanical sympathy for this engine so for almost 18,000m I think its held up pretty well but it was certainly ready for a refresh.

Piston skirts and bores were in great condition which is a testament to Galloway's fantastic engineering work. The wall of the dropped valve cylinder is damaged but I'm hoping an oversize rebore will sort that. I'll see what my local engineering shop has to say about that.

The current plan if the block is salvageable is for a set of CP 100.5mm pistons (purely because of the sleeved block), new heads, Ferrea valves and currentGTX35R turbo fixed by AET Turbos.

If the block is goosed then I'll have to bite the bullet and go the 2.35 route but I really can't afford one of the blocks at the mo so it will have to wait a few months.





























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Last edited by dazdavies; 15-10-2017 at 09:21 PM.
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